Colin
Retired.
- Joined
- Sep 17, 2017
- Messages
- 1,663
- Reaction score
- 2,541
- Location
- Huddersfield.
- Hardiness Zone
- 7
- Country
Hi,
Bron kindly bought me this Hyundai 139cc HYT140 tiller/rotavator brand new for Christmas last year and its a beauty; eventually the ground dried sufficiently to use it in anger; I had spade dug the entire area to be rotavated removing many roots and a mountain of stones but after a session whilst cleaning the rotavator I noticed a tine was displaced. The tine had pivoted around its securing rivet rising out of the indents in the driving flange.
After a struggle I managed to force the tine back home but when used again the same thing happened. Today I decided to sort this problem out once and for all. I removed both tine assemblies and in the workshop arc welded the tines to the driving flanges; a simple and quick repair to anyone with access to a welder. Each tine unit is held in position by a single 8mm set screw and locking nut. I always spend time after using any of my kit to clean and lubricate if needed then it's ready for action.
Once I got the knack of using this rotavator its a pleasure to rotavate rather than spade digging.
Kind regards, Colin.
My new toy.
Tine assemblies.
Tine assemblies removed ready for repairing.
The tine at the top of the picture should be vertical but it's pivoted on its rivet; care is needed forcing one of these tines back into position due to the force required; not the easiest of things to handle.
A quick and easy arc welding job; a going over with a wire brush and a blast of black paint from a rattle can its now better than new.
Bron kindly bought me this Hyundai 139cc HYT140 tiller/rotavator brand new for Christmas last year and its a beauty; eventually the ground dried sufficiently to use it in anger; I had spade dug the entire area to be rotavated removing many roots and a mountain of stones but after a session whilst cleaning the rotavator I noticed a tine was displaced. The tine had pivoted around its securing rivet rising out of the indents in the driving flange.
After a struggle I managed to force the tine back home but when used again the same thing happened. Today I decided to sort this problem out once and for all. I removed both tine assemblies and in the workshop arc welded the tines to the driving flanges; a simple and quick repair to anyone with access to a welder. Each tine unit is held in position by a single 8mm set screw and locking nut. I always spend time after using any of my kit to clean and lubricate if needed then it's ready for action.
Once I got the knack of using this rotavator its a pleasure to rotavate rather than spade digging.
Kind regards, Colin.
My new toy.
Tine assemblies.
Tine assemblies removed ready for repairing.
The tine at the top of the picture should be vertical but it's pivoted on its rivet; care is needed forcing one of these tines back into position due to the force required; not the easiest of things to handle.
A quick and easy arc welding job; a going over with a wire brush and a blast of black paint from a rattle can its now better than new.